well got it out on the water and as we all know when a mechainc is present the problems do not arise, gladly this was not the case....
got it out on the water and the mechanic make some adjustments to the throttle linkages and a very slight timing adjustment and it runs alot smoother and responds to throttle very very well, luckily he has told me that it has had a recent rebuild as he could tell from the way the engine looked, responded and power it produced..
he seems to think it is a 115hp as he thinks that a 90hp would not go like mine does, the previous owner told me it was a 115 but i saw the tag on the carby and it says 90hp, there is no model number as during the rebuild someone had replaced the welsh plug that its usually stamped on....
starting warm after sitting for a while still was a issue and he is convinced that it is actually my control box as there is ALOT of play in my throttle lever....he susgested that after sitting for a while that it would start first go if throttle was applied, he showed me that if i gave it more throttle that my lever was allowing using the engine linkages it fired up first go and when reduced to normal idle it was perfect.
i towed it home and just finished fiddling with it and it seems that inside the control box, there is no adjustment inside so i had a play with the cable myself on the engine side, i tightened up all moving parts inside the control box and there is alot less free play now but i am still convinced that the box is the culprit...
im pretty sure that on other boats if you rev the motor via the throttle leaver you can get a very high idle, mine is not the case, it barley moves the throttle, if it could move more it would act like a normal boat.
i have got the motor to start MUCH easier using the adjusted throttle leaver, it has more revs than it had before fully open and when dropped it returns to normal idle... i will be testing it on saturday when i go fishing....
another problem arose whilst i was playing with the motor on the muffs, the overheat buzzer in the controller turned on while idling for around 5 mins. i rang the mechanic and he says that it was peeing water well on the river, he seems to think its the muffs, and water pressure, as it takes around 25 seconds for water to come out the tel tale. but it comes out cold compared to the exhaust...
ive ordered a new water pump kit for reassurance and i will change it tomorrow....
but so far so good and im pleased that its not any costly drama, will have a proper test while fishing on sat all day...